Han, Je-Chin2010-01-152010-01-162017-04-072010-01-152010-01-162017-04-072009-082010-01-14http://hdl.handle.net/1969.1/ETD-TAMU-2009-08-2927The research focuses on testing the film cooling effectiveness on a gas turbine blade suction side surface. The test is performed on a five bladed cascade with a blow down facility. Four different blowing ratios are used in this study, which are 0.5, 1.0, 1.6, and 2.0; mainstream flow conditions are maintained at exit Mach number of 0.7, 1.1 and 1.3. Nitrogen is injected as the coolant so that the oxygen concentration levels can be obtained for the test surface. Based on mass transfer analogy, film cooling effectiveness can be computed with pressure sensitive paint (PSP) technique. The effect of blowing ratio on film cooling effectiveness is presented for each testing condition. The spanwise averaged effectiveness for each case is also presented to compare the blowing ratio and mainstream effect on film cooling effectiveness. Results show that due to effects of shock, the optimum blowing ratio is 1.6 for exit Mach number of 1.1 and 1.3; however; without the effects of shock, the optimum blowing ratio is 1.0 for exit Mach number of 0.7.en-USfilm coolingblowing ratioBlowing Ratio Effects on Film Cooling EffectivenessBook